1981-02-01

Noise and Performance of General Aviation Aircraft: A Review of the MIT Study 810586

The primary objective of the study was to explore the possibility of reducing noise from a general-aviation-type propeller without altering significantly its aerodynamic performance or the engine characteristics. Our study of this possibility involved aerodynamic and acoustic theory, design, construction, and wind tunnel testing of model propellers, design and manufacture of full-scale propellers, and, finally, flight tests. One propeller exhibited an overall measured reduction of 4.8 dBA during a flight test. This reduction was achieved with minimal changes in performance.

SAE MOBILUS

Subscribers can view annotate, and download all of SAE's content. Learn More »

Access SAE MOBILUS »

Members save up to 16% off list price.
Login to see discount.
Special Offer: Download multiple Technical Papers each year? TechSelect is a cost-effective subscription option to select and download 12-100 full-text Technical Papers per year. Find more information here.
We also recommend:
TECHNICAL PAPER

Impact of Advanced Propeller Technology on Aircraft/Mission Characteristics of Several General Aviation Aircraft

810584

View Details

TECHNICAL PAPER

A High Efficiency Fuselage Propeller (”Fusefan”) for Subsonic Aircraft

1999-01-5569

View Details

JOURNAL ARTICLE

Airbus AI-PX7 CROR Design Features and Aerodynamics

2013-01-2245

View Details

X